8229_reboot
Polar spacecraft anomaly: On August 2 (Day 214/20:26), an anomaly occurred in the primary Command and Attitude Processor (CAP). The problem manifested itself in the inability of the spacecraft to respond to normal ground commands. To regain control, a soft boot of the CAP was executed by a direct command to the processor, bypassing the normal command path. Resetting the CAP required the reloading into memory of all spacecraft and instrument macros, as well as the stored command table. Following restoration of the CAP and regaining valid telemetry, the power system mode controller was found to have switched from the primary to the secondary side; the system was restored manually to the primary side. Evaluation of spacecraft and instrument telemetry showed that main power had not been interrupted to spacecraft subsystems or instruments, despite the automatic switch to the secondary power system mode controller. However, normal operation of the despun platform was interrupted, the battery V/T levels were changed, and the spacecraft clock was reset to 1995. In addition, the HYDRA instrument showed both high and low voltage systems to be in the off state; the TIDE high voltage was also in the off state. In both these cases, the main power remained on. Immediately after restoring command capability, the clock was reset manually to GMT, and the battery V/T levels reset to nominal. The VIS instrument scientist elected to place the instrument in a safe state. In addition, the UVI filter wheel was placed in the "home" position to close the optical path; the instrument remained in operation. CAMMICE, CEPPAD, MFE, PIXIE, SEPS, EFI, and TIMAS reported the instruments to be operating normally following the anomaly. On August 5, the despun platform was reconfigured for normal operation and calibrated. HYDRA was restored to operation on August 4, TIDE on August 5, and VIS on August 6. The UVI filter wheel was set for normal operation on August 5, following reconfiguration of the despun platform. A subsequent report from EFI indicated that the instrument was in an unusual state. A power off reset was executed on August 4 to return EFI to a known state before being configured for normal operation. The CEPPAD IPS sensor was later reported to have been reset to the default Table 0 mode; the normal operating mode uses Table 5. The spacecraft and all instruments are now in full operation, with no lasting effects evident. NOAA's Space Environments Center reported a large solar flare occurring close to the time of the anomaly. We presume this to be the cause of the upset of the spacecraft subsystems. John Wainwright 8/11/99